Friday, March 13, 2020

Closer Look At An Enerplus Turtle Well -- The Map Well -- March 13, 2020

The well:
  • 35065, 520, was SI/NC-->conf, Enerplus Map 152-94-33D-28H-TF1, Antelope, t9/19; cum 141K 1/20; F; 43 stages; 15.6 million lbs; (there is a common map turtle),
Production:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
SANISH1-20203038138381061603660907511679629
SANISH12-201931420334196923828671263911427916
SANISH11-201927320333177219060511573817112618
SANISH10-201916142841439121489228131069112086
SANISH9-20191314606144092812729212510924077

From the file report:
  • spud: January 12, 2019
  • TD: May 10, 2019;
  • total days: 18
  • total drilling days: 178.2
  • True Rig 40
  • vertical section: 9,833.9 at TD;
  • KOP: 10,173' TVD;
  • lateral footage: 10,096';
  • it looks like it took about 1.5 days to drill the curve; it took two extra trips during the curve due to lack of build rates;
  • slightly less than full four days to drill the lateral; no trips occurred in the lateral portion;
  • background gas ranged from 500 - 1600 units; connection gases ranged from 800 - 2400 units;
Separation Factor Plot (two screenshots to get this big enough to be seen):


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