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Saturday, October 3, 2020

An Old MRO Well With 80X Jump In Production -- October 3, 2020

The well:

  • 17568, 539, MRO, Charles Shobe - USA 44-18H, Reunion Bay, 10' target, middle Bakken, t2/09; cum 538K 8/20; well was extended approximately 940' in 2018; open hole frack, 2009 with 500,000 lbs sand; re-fracked 7/16/2018 - 7/26/2018; 45 stages; 5.5 million lbs proppant; one more stage 1/25/2019; 526,000 lbs; IP with re-frack: 5,645 bbls;

Full production profile at this post.

Production jump in 2019:

  • 38,867 bbls over 18 days extrapolates to 64,778 bbls
  • prior to jump in production: about 800 bbls/month
  • after jump in production: 64,778 bbls / month
  • 64,778 / 800 = 80x
  • and a very, very small re-frack in conjunction with fracking neighboring devopment / infill wells; 
BAKKEN7-2019311134411370497821331342017223
BAKKEN6-2019301271012517464013795013031
BAKKEN5-2019311567715763583930905029970
BAKKEN4-2019301777517769495131918030875
BAKKEN3-2019312268522491590149314047976
BAKKEN2-2019261557415825541721418020345
BAKKEN1-20193136180361651078950286047817
BAKKEN12-20181831554316461090240232038220
BAKKEN11-20181525449253391035630770030603
BAKKEN10-20181838867399892466947393047308
BAKKEN9-20181229459280213283332716032596
BAKKEN8-201810171498098
BAKKEN7-20181100000
BAKKEN6-20180000000
BAKKEN5-201800710000
BAKKEN4-20182351951754620356127
BAKKEN3-20183170872870897256470
BAKKEN2-2018226236456475534585

 Initial production back in 2008 after first open-hole frack:

BAKKEN12-20091413611100342134101341
BAKKEN11-20092323302773282230602306
BAKKEN10-20093139914041247393003930
BAKKEN9-20093041153983233405204052
BAKKEN8-20093146144661272454804548
BAKKEN7-20093141333788408407104071
BAKKEN6-20092660916496652600606006
BAKKEN5-20093146554631437458404584
BAKKEN4-20093043524243313428604286
BAKKEN3-20093157365580508562905629
BAKKEN2-200928852384771280811408114
BAKKEN1-200919232718341438190301903
BAKKEN12-2008415017512012

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