Pages

Tuesday, March 31, 2020

Random Look At The "Halo" Effect In The Bakken -- March 31, 2020

Four huge Kraken wells were fracked/stimulate/tested on/about July, 2020. These four wells "cut right across" an old Kraken well, almost perfectly perpendicularly. Note the "halo" effect on the old Kraken well, #22563. This old well, by the way, is an incredibly short horizontal, coming in at only 14,626 feet TD..

The wells:
  • 36010, 860, Kraken, Bigfoot 23-11 LW 1H, Sanish, t7/19; cum 206K 1/20; a 46K month;
  • 36011, 902, Kraken, Bigfoot 23-11 2TFH, Sanish, t7/19; cum 170K 1/20; a 31K month;
  • 36012, 1,748, Kraken, Bigfoot 23-11 3H, Sanish, t7/19; cum 254K 1/20; a 54K month;
  • 36013, 1,564, Kraken, Bigfoot 23-11 4TFH, Sanish, t7/19; cum 224K 1/20; a 41K month;
The old well:
  • 22563, 704, Kraken, Hukkanen 11-23H, Sanish, t6/12; cum 168K 1/20;
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN1-202029257826672348303917101100
BAKKEN12-2019303152347631253716693404
BAKKEN11-20193036223477337142704503613
BAKKEN10-2019313915429637804745874441
BAKKEN9-20191414666691273177701705
BAKKEN8-2019116223701960196
BAKKEN7-20190000000
BAKKEN6-20190000000
BAKKEN5-201914805592528
BAKKEN4-201927623748195755463127
BAKKEN3-2019316887081858936760
BAKKEN2-20192862646219711577930
BAKKEN1-2019317229842239116660

The graphic:


What about those two other older wells? Glad you asked:
  • 22853, 687, Kraken, Isaac 11-23H, Sanish, t7/12; cum 144K 1/20; "halo effect"; jump from 600 bbls/month to 2,800 bbl/smonth;
  • 16935, 780, Kraken, Frandson 11-23H, Sanish, t6/08; cum 144K 1/20; "halo effect" less noticeable, and did not last as long, from 750 bbls/month, to 2,500 bbls/month, but quickly dropped back to 986 bbls in January, 2020;

No comments:

Post a Comment

Note: Only a member of this blog may post a comment.