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Sunday, February 16, 2020

The WPX Good Voice/Benson Wells In Spotted Horn Have Been Updated -- February 16, 2020

Link here.

The most recent well was completed in late 2018/early 2019, and tested 1/19.

Following that completion, this well reported a significant jump in production. Note the small IP, and then note that this well will soon hit 500K; about six years old; jump in production:
  • 27068, 502, WPX, Good Voice 34-27HD, Squaw Creek, t11/14; cum 464K 12/19; off line while neighboring wells fracked; off line for about five months; now back on line as of 1/19;
Production during period of interest:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN12-201931644264232066874259181764
BAKKEN11-201930634664791699861310826358
BAKKEN10-201931505350454923685712754539
BAKKEN9-201930487850013731661912764329
BAKKEN8-201931427939704133580732051633
BAKKEN7-2019181189118510721494629421
BAKKEN6-20192017141728132621551439184
BAKKEN5-201931393439143208494428751224
BAKKEN4-201930464146342711583428302106
BAKKEN3-2019292840281534713399127870
BAKKEN2-2019282313230412211282107430
BAKKEN1-2019111091108546348130870
BAKKEN12-20180000000
BAKKEN11-20180000000

Off line from late 8/18 to late 1/19.

BAKKEN7-20181211401184351448642010
BAKKEN6-2018303069305579711497108170
BAKKEN5-201831341534928411015394200
BAKKEN4-20183033603278958662259080
BAKKEN3-2018313822389087111133103570

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