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Monday, November 18, 2019

Monday Morning, Halo Effect, #4 -- MRO -- #17502 -- November 18, 2019

And this old well recently went over 500,000 bbls cumulative

The well:
  • 17502, 637, MRO, Mark Sandstrom 14-32H, Reunion Bay, t12/08; cum 546K 3/20; off line 3/20; remains off line 4/20;
Production period of interest:
BAKKEN8-20153174707596182096357780870
BAKKEN7-20153174657384187596518420246
BAKKEN6-201530767677341948847255231949
BAKKEN5-201531870684802335775215495094
BAKKEN4-20151125292596765221001884
BAKKEN3-201531103311040031339044577707
BAKKEN2-20152810389103493001926037995
BAKKEN1-2015311310613103405511737010151
BAKKEN12-2014311634716237577014037012104
BAKKEN11-2014301985720389755217157314864
BAKKEN10-20143126140259931202322191519208
BAKKEN9-20142614450144081137812315010620
BAKKEN8-20143120932205561255019364155515385
BAKKEN7-20140000000
BAKKEN6-20141122532100
BAKKEN5-20140000000
BAKKEN4-20141914071721182129901038
BAKKEN3-2014312391207124730791879759

This well was drilled back in 2008. Wow, the Bakken was just getting started. This was a pretty good well by "2008" standards. Then six years later, in 2014, it got "really good." A delayed gusher. LOL.

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