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Sunday, March 11, 2018

Random Update Of An Old WPX Bear Den Well, #20359 -- March 11, 2018

I'm not sure what resulted in the jump in production. According to FracFocus this well has been fracked only once, back in 2011. Note the production jump in late 2015, note, it was never taken off-line during that period (in bold red). The legal name of the well suggests a second bench TF, but in fact it's a middle Bakken well. No neighboring wells were fracked during the period of increased production.The well:
  • 20359, 96 (no typo), WPX, Bear Den 24-13H2, middle Bakken, 12 stages; 2.7 million lbs; t 10/11; cum 465K 1/18;
BAKKEN10-20163174217575244893297329599
BAKKEN9-201630790677612681993773371149
BAKKEN8-201631855485123011107538764442
BAKKEN7-20162777007655292696797476884
BAKKEN6-201630793379463152997069351575
BAKKEN5-2016319368936243011177786671474
BAKKEN4-2016308442839549071061176611374
BAKKEN3-20162429822982541137491993899
BAKKEN2-20162424662483595131002225113
BAKKEN1-2016319066911943791139570622668
BAKKEN12-201531101601023055361262350405813
BAKKEN11-20153099751006267631253890891714
BAKKEN10-201531109981076390301382593612751
BAKKEN9-20153097769861101511228883182401
BAKKEN8-20152316031539584223355391450
BAKKEN7-20153031553057100545983030747

Interestingly enough, there is a sundry form received in October, 2015, that said that there was an overflow of produced water due to a mechanical problem with the pump. It makes me think the well was being re-worked about that time but nothing was found in the file report. Not only was there a jump in production back  in late 2015, that increase in production held on for quite some time.

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