Tuesday, February 4, 2020

Two Wells No Longer Being Followed -- Back On Line And Doing Great --February 4, 2020

These two wells have been removed from the list of wells that need to be followed. They are clearly back on line and are still great wells:
May 19, 2019: on 320-acre spacing; these are the only two wells on this drilling unit; they both went inactive 1/19; remain inactive 3/19:
  • 20307, in the west half, A/1,328, EOG, Clarks Creek 103-17H, Antelope, Sanish pool, t11/11; cum 157K 10/19; only 1,000 bbls/month; off line as of 1/19; still inactive, 7/19; 4 days, 8/19; looks to be back on status as of 9/19;
  • 19693, in the east half, 722, Enerplus, Danks 17-44H, Antelope, Sanish pool, t7/11; cum 263K 10/19;  only 1,000 bbls/month; off line as of 1/19; still inactive, 3/19; active as of 4/19 but only producing one day/month? see this note. And here. Now back up to 4,000 bbls/month with only one day of being on line according to the scout ticket; see this post; strange production profile; again, only one day of production 8/19; only one day of production, 9/19 but produced 3,479 bbls; one day, 10/19, 2,207 bbls;
Recent production for #20307:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
SANISH12-201924111310976321508593598
SANISH11-2019301770179799024221545469
SANISH10-201931226622641542368515041761
SANISH9-20193016541648173523277871132
SANISH8-201946040571230
SANISH7-20190000000
SANISH6-20190000000
SANISH5-20190000000
SANISH4-20190000000
SANISH3-20190000000
SANISH2-20190000000
SANISH1-2019236656113201331344674
SANISH12-2018319169533591920894604
SANISH11-2018309429624211794778608

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