Friday, April 3, 2015

Another Example Of Choked Back Wells -- North Dakota -- April 3, 2015

There is a lot of activity in this area and it's always possible the well was taken off-line for operational or flaring reason, but note that after a great January, 2015, the well was only on-line for 9 days in February:
  • 27579, 1,920, BR, Sequoia 31-4MBH, Hawkeye, t9/14; cum 43K 2/15:
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN2-2015988188841140510972109620
BAKKEN1-2015302033520107393225295217553511
BAKKEN12-20140000000
BAKKEN11-20140000000
BAKKEN10-20141000200
BAKKEN9-2014251396213962411321999021937

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Another BR Sequoia well off-line for much of February; maybe for operational reasons. Imagine the production if on-line for a full month:
  • 27578, 1,296, BR, Sequoia 31-4TFH, Hawkeye, t9/14; cum 34K 2/15;
PoolDateDaysBBLS OilRunsBBLS WaterMCF ProdMCF SoldVent/Flare
BAKKEN2-2015151278512730333813602135860
BAKKEN1-20152010998110822359985098320
BAKKEN12-20140000000
BAKKEN11-2014120700200
BAKKEN10-2014199611880118201179
BAKKEN9-20148884586532050136386313555
 

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